Stumble Pop Update

They found the engine ran really rough on just the right magneto and that EGT#1 went blank. They took it apart a bit to test the leads and the plugs but found no issues. Put it back together again and it ran great.

So the thinking is that taking it apart knocked a bit of lead or other contaminent out that was causing the issue.

We also found that we have fine wire spark plugs and plan to replace them with Tempest massives, due to this. The Platinum Aviation blog has some great spark plug info here too.

Comments

Popular posts from this blog

Updating data on the Garmin Perspective system

Hiking to Rocky Peak in Steamboat Springs

G1000 transistion training - emergencies - final flight